Filled the car to the brim with petrol to dilute any stale petrol and have adjusted the slow running jets along the lines suggested by my friendly MOT mechanic so hopefully a run at the weekend will show the benefits. I've adjusted the auto-box kick-down cable as far as the screw adjuster allows and that's certainly lowered the speed of 2nd to 3rd changes by 10mph. I've started making a new link between the throttle and kick-down cables that should allow me to reclaim some of the screw adjustment and hopefully further improvements.
Made some running repairs to the exhaust which got an advisory for being loose at he MOT. Tightening up one clamp just sheared the corroded U-bolt so as a temporary fix a couple of replacements from Halfords were fitted. A long term solution is needed when funds allow.
I've also started fabricating a cowl between grill and radiator, partly to see if it channels the air through the radiator better and partly to improve the cosmetics of this area. Outside cosmetics were also improved yesterday by washing off the winters dust and giving it a polish. It comes up quite well but does highlight more jobs to do next winter.
Today I changed the oil filter and oil ready for this years outings which start this weekend with the South Midlands "Blossom Trail" run. With the to & from miles and the 50 mile route well see if we manage 75 miles without any problems




